ASN Wikibase Occurrence # 292647
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Date: | Monday 6 February 2006 |
Time: | 10:25 LT |
Type: | Lancair 360A |
Owner/operator: | Private |
Registration: | N15KH |
MSN: | 001 |
Total airframe hrs: | 770 hours |
Engine model: | Lycoming IO-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Thermal, California -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Palm Springs International Airport, CA (PSP/KPSP) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane collided with power lines during a forced landing following a loss of engine power. The pilot reported that while maneuvering at 2,000 feet the engine began losing power. The pilot decided to divert to a nearby airport to make the emergency landing. While en route to the alternate airport, the pilot observed a part of the engine departing through the cowling and the engine lost complete power. At that point he knew he was not going to make it to the airport and decided to make a forced landing on a highway. Examination of the engine showed that the number three cylinder separated from the crankcase at the mounting pad due to the separation of its mechanical attachments. Once the cylinder separated, the piston then became unsupported, which resulted in the subsequent separation of the connecting rod from the crankshaft journal. Severe fretting signatures were found on the cylinder flange and crankcase mounting pad. The threads on the top hold down studs were undamaged and indicated that these nuts became loose and backed off. The studs on the bottom of the cylinder were fractured in overload and separated at a level consistent with the upper surface of the cylinder mounting flange.
Probable Cause: A loss of engine power caused by the separation of the number three cylinder due to the improper torque on the hold down nuts.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX06LA103 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB LAX06LA103
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 07:14 |
ASN Update Bot |
Added |
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