ASN Wikibase Occurrence # 293120
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 1 September 2005 |
Time: | 20:30 LT |
Type: | Ballhagen/shyrock Q-2 |
Owner/operator: | Private |
Registration: | N12QJ |
MSN: | A2876 |
Total airframe hrs: | 300 hours |
Engine model: | Subaru EA81-1.8L |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kalispell, Montana -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Kalispell, MT (MT95) |
Destination airport: | (MT95) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Just prior to the flight, the pilot, who was five hours into a ten hour experimental aircraft flight test regimen, readjusted the valve lash in the Subaru engine that powered the subject aircraft. At the beginning of the flight, he took off and climbed to about 1,000 feet above ground level (agl). After he rolled out on downwind, his ground crew contacted him on the aircraft radio to advise him that the aircraft's engine appeared to have been missing and running rough during the takeoff and initial climbout. About the time that the pilot received the radio transmission, the aircraft's engine quit producing power, and he decided to continue on around the pattern in order to execute a forced landing on the runway from which he had departed. As he turned from base to final, the pilot realized that he might not be able to stretch the glide to the end of the runway, but he elected to attempt to do so. When the aircraft descended to about 25 feet agl, its airspeed slowed to the point where it stall/mushed into the terrain about one-quarter of a mile off the end of the runway. In a post accident inspection, it was determined that the valve clearance in the engine had been set with a gap so small that when the internal engine temperature began to increase the exhaust valves in each cylinder did not completely close. Without the closure of the valves, sufficient compression was not created in the cylinders, and the engine stopped producing power.
Probable Cause: The pilot/owner's improper setting of the engine's valve clearance, leading to the failure of the exhaust valves to fully close and a total loss of power while on a VFR downwind, and the pilot/owner's failure to maintain sufficient airspeed as he tried to extend his power-off glide to the approach end of the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA05LA189 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB SEA05LA189
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 16:19 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation