Accident Bellanca 8GCBC N87008,
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ASN Wikibase Occurrence # 293295
 
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Date:Monday 25 July 2005
Time:18:50 LT
Type:Silhouette image of generic BL8 model; specific model in this crash may look slightly different    
Bellanca 8GCBC
Owner/operator:David G Martin
Registration: N87008
MSN: 51-74
Total airframe hrs:1587 hours
Engine model:Lycoming O-360
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Oroville, California -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Oroville, CA
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane nosed over during landing. The pilot said he had been out practicing landings, and the accident landing was to be his last of the day. The first three landings were completed with no discrepancies. On the fourth landing, the airplane touched down on the main landing gear in a tail low attitude; the tail started to rise, and the pilot thought that the main landing gear "appeared to make a slight 'bounce.'" He did a go-around and came back to land for the last time. On the accident landing, he did a 3-point landing. The landing was normal, power was at idle, and he noted his airspeed at 65 miles per hour; however, it felt as if the brakes were being "strongly applied." The tail started to rise, and he immediately pulled back on the stick to its full rearward position. He checked his foot position on the rudder pedals, and removed them temporarily to see if that would help; however, the braking action continued with no airplane response to the full aft stick. The airplane rotated forward, and nosed over. The pilot stated that after the accident he walked the runway and saw that the main landing gear left straight skid marks for about 150 feet from the touchdown point, until the airplane nosed over. A witness observed black smoke coming from the wheels just after the airplane came to rest inverted. Another witness was at the airplane about 25 minutes after the accident and attempted to rotate the main wheels. The witness said that they would rotate, but that there was "quite a bit of drag on them." Two airframe and power plant mechanics examined the airplane the day after the accident and found no identifiable brake system anomalies. They noted that the parking brake was in the OFF position, and indicated that the skid marks on the runway were indicative of the brakes either partially or fully activated on touchdown until the airplane turned over. They theorized that the brake anomaly might have been due to the brake piston being stuck, possible foreign debris in the brake lines or brakes themselves, or a high ambient temperature causing internal hydraulic pressure buildup in the cylinder and lines, thus activating the brakes.

Probable Cause: a binding and/or activation of the brakes that lead to an inadvertent nose over. The underlying root cause of the brake binding/activation could not be determined.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX05LA245
Status: Investigation completed
Duration: 1 year and 10 months
Download report: Final report

Sources:

NTSB LAX05LA245

Revision history:

Date/timeContributorUpdates
09-Oct-2022 18:24 ASN Update Bot Added

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