Fuel exhaustion Accident Bell 206B N27VT,
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ASN Wikibase Occurrence # 293363
 
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Date:Tuesday 12 July 2005
Time:12:32 LT
Type:Silhouette image of generic B06 model; specific model in this crash may look slightly different    
Bell 206B
Owner/operator:Wilfred Quinones
Registration: N27VT
MSN: 3070
Year of manufacture:1980
Engine model:Allison 250-C20B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:San Juan, Puerto Rico -   United States of America
Phase: Unknown
Nature:Private
Departure airport:San Juan-Fernando Luis Ribas Dominicci Airport (SIG/TJIG)
Destination airport:San Juan-Fernando Luis Ribas Dominicci Airport (SIG/TJIG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that earlier in the morning he flew with an individual for 1/2 hour, and following that flight secured the engine and waited for approximately 1 hour to allow the engine to cool down. Following that time, he started the engine in order to relocate the helicopter to the south side of the airport. While air taxiing, he suddenly saw the boost pump caution light illuminate followed by the engine out light and low rpm warning lights. He performed an autorotation on the south taxiway. According to the passenger, while flying 10 feet above ground level the engine seemed to start losing power. The pilot maneuvered the helicopter into the wind while descending, and further reported that when the helicopter contacted the ground, the main rotor blade contacted the tailboom causing separation of it. The pilot then secured the helicopter and asked if he was OK. Both exited the helicopter, and rescue personnel assisted them promptly. The passenger also stated that the total flight time was approximately 20-30 seconds, and at no time did he perceive any visual or audio alarms, but he is not familiar with the helicopter or its systems. According to the Federal Aviation Administration (FAA) inspector-in-charge (IIC) who examined the accident site and helicopter, and also talked with the pilot, the pilot reported to him that the purpose of the flight was to reposition the helicopter for fuel. The pilot reported to the FAA-IIC that during his preflight inspection, the fuel gauge indicated greater than 10 gallons of fuel. Postaccident examination of the helicopter revealed less than one ounce of fuel was drained from the fuel tank, and approximately 1 liter of fuel was drained from the fuel filter canister. The fuel quantity gauge was tested and was found to indicate correct when fuel was added in five gallon increments; a total of 15 gallons were added during the test.

Probable Cause: The inadequate preflight/planning by the pilot for his initiation of the flight with inadequate fuel supply, and his failure to maintain main rotor rpm following a total loss of engine power due to fuel exhaustion which resulted in a hard landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA05CA134
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB MIA05CA134

History of this aircraft

Other occurrences involving this aircraft
28 September 1995 N28SJ Sajalasi Corp 0 Indianapolis, IN sub

Revision history:

Date/timeContributorUpdates
09-Oct-2022 19:11 ASN Update Bot Added

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