ASN Wikibase Occurrence # 293375
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Date: | Saturday 9 July 2005 |
Time: | 10:50 LT |
Type: | Cessna 210E |
Owner/operator: | Private |
Registration: | N4933U |
MSN: | 21058633 |
Year of manufacture: | 1965 |
Total airframe hrs: | 3112 hours |
Engine model: | Continental IO-520A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | La Gygne, Kansas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Gardner, KS (K81) |
Destination airport: | Ozark, MO (2K2) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was landed in a corn field following a loss of engine power while in cruise flight. The pilot reported that upon reaching 7,500 feet he was adjusting the engine to cruise power, when the engine went to idle. He reported that he pulled the throttle out, pushed it back in and got a "little power surge." He stated that there was no change in power when he adjusted the throttle a second time. The pilot reported, "I attempted a third time and it came out of the dash (about a foot)." He reported that he threaded the cable back into the instrument panel and established communications with air traffic control. The pilot was given a vector to the closest airport and upon reaching an altitude of 3,000 to 3,500 feet, realized the airport was too far away and that he needed to pick a field in which to land. The pilot stated he selected a corn field and made a "textbook" landing, but the airplane "weathervaned" shortly after touching down. The pilot stated, "I informed them [air traffic control] that the airplane looked to be in pretty good shape, not realizing the amount of damage that corn can do to sheet metal!" The throttle cable was removed from the airplane and examined at the National Transportation Safety Board's Materials Laboratory. Examination revealed that both the stranded cable and the inner spring failed as a result of wear followed by fatigue cracking. Both the brass tube end of the assembly and the inner plunger showed an area of wear. The source of the wear could not be determined.
Probable Cause: The failure of the throttle control cable which resulted from wear followed by fatigue cracking. A factor associated with the accident was the corn crop which the airplane contacted during the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI05LA178 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB CHI05LA178
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 19:22 |
ASN Update Bot |
Added |
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