ASN Wikibase Occurrence # 293444
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Date: | Saturday 6 November 2004 |
Time: | 10:45 LT |
Type: | Cessna 150M |
Owner/operator: | Stebbins Aviation Inc |
Registration: | N704KX |
MSN: | 15078682 |
Year of manufacture: | 1976 |
Total airframe hrs: | 9986 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Longview, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Longview-East Texas Regional Airport, TX (GGG/KGGG) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The 93-hour private pilot contacted approach control, at the East Texas Regional The 93-hour private pilot contacted approach control, at the East Texas Regional Airport (GGG), with the intention of landing. After being handed over to the control tower and while approximately four miles west of the airport, the engine experienced an un-commanded reduction of power from 2,500 revolutions per minute (RPM) to approximately 1,000 RPM. The pilot tried moving the throttle to different positions, but was unable to change the RPM. Reporting the engine problem to the control tower, the pilot was cleared to land "any runway and any direction." Unable to make the airport, the pilot elected to land in a field. At approximately 50 feet above ground level (agl), the engine experienced a momentary burst of power and then returned to approximately 1,000 rpm. Committed to land, the pilot turned off the engine ignition switch and directed the airplane between two trees in an attempt to reach a suitable landing field. While maneuvering through the trees, the outer right wing contacted a tree and shortly thereafter the airplane settled to the ground, coming to rest in an upright position. According to a Federal Aviation Administration (FAA) inspector, who responded to the accident site, both fuel tanks were intact and contained residual fuel. Approximately one inch of fuel was sumped from each fuel tank and there was no evidence of any fuel spill or leaks at the accident site.
Probable Cause: The pilot's improper inflight planning which resulted in a loss of engine power due to fuel exhaustion. A factor was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW05LA023 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB DFW05LA023
Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 05:54 |
ASN Update Bot |
Added |
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