ASN Wikibase Occurrence # 293565
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 23 June 2005 |
Time: | 16:13 LT |
Type: | Titan Aircraft Tornado |
Owner/operator: | Private |
Registration: | UNREG |
MSN: | T00503S0HK0375 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Bath, Pennsylvania -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Moore Township, NJ |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot owner completed a preflight inspection of his unregistered, homebuilt airplane, and departed from the airstrip. The rotation and takeoff were at their customary points on the strip, and the airplane climbed on a "normal gradient." About 400 feet above ground level, the engine "burbled," and then the airplane "rocked a little" in the pitch and roll axis. The engine continued the burbling sound as it ran, and the airplane continued flying for 10 to 12 seconds before it "fell off on the left wing," descending almost vertically to the ground. Examination of the two-cylinder engine revealed that the forward spark plug of the rear cylinder was still attached to its ignition lead, but the plug was not installed, and hung next to the cylinder. The spark plug remained completely intact. Examination of the corresponding cast aluminum spark plug hole revealed stripped threads. The plug was reinserted into the hole, moved "side to side," and then withdrawn from the hole by hand. The pilot held a private pilot certificate with a rating for airplane single engine land. His most recent application for a medical certificate was denied 16 years before the accident for "Administrative or Legal" reasons. The pilot reported 110 hours of total flight experience on that date.
Probable Cause: The pilot/owner's failure to maintain adequate airspeed following a loss of engine power, which resulted in an inadvertent stall/spin. Factors in the accident were the stripped spark plug threads, and an inadequate preflight inspection by the pilot/owner.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD05LA083 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB IAD05LA083
Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 07:43 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation