ASN Wikibase Occurrence # 293604
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Date: | Friday 17 June 2005 |
Time: | 08:05 LT |
Type: | Piper PA-32-300 |
Owner/operator: | Jerald L Robinson |
Registration: | N646RM |
MSN: | 32-40087 |
Year of manufacture: | 1966 |
Total airframe hrs: | 3182 hours |
Engine model: | Lycoming IO-540-K1A5 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Myers, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Naples Airport, FL (APF/KAPF) |
Destination airport: | Asheville Regional Airport, NC (AVL/KAVL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was climbing after takeoff, and the pilot heard and felt a change in the engine operation. He stated the oil pressure gauge and the oil temperature gauge showed normal readings, but the engine rpm spiked briefly beyond redline then returned to a lower rpm. The pilot headed towards the nearest airport. He stated then "something gave in the engine, and it began to vibrate the yoke. A little further, and oil began to splatter on the windshield." The propeller continued to turn, the airplane could not maintain altitude, and the pilot glided it until it descended into trees and a swamp. Examination of the engine revealed cracks and a hole in the top of the crankcase. The No. 5 connecting rod cap was separated, pieces of the rod cap and bolts were in the engine sump, and the fracture features of the rod cap and bolts were obscured by mechanical damage. No evidence of oil leakage from any engine seals or at the propeller hub was observed. The connecting rods had been replaced during an engine major overhaul completed July 13, 1992. A new McCauley propeller was installed in accordance with Supplemental Type Certificate SA433CH on April 14, 2005, and an annual inspection was completed on the same date at an engine time since major overhaul of 1141.2 hours. The engine had accumulated 9 hours since the annual inspection, and the pilot reported there were no engine anomalies during those flights.
Probable Cause: A loss of engine power due to the connecting rod cap separation for undetermined reasons. Related factors were trees and the swampy terrain condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL05LA101 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB ATL05LA101
Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 08:12 |
ASN Update Bot |
Added |
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