ASN Wikibase Occurrence # 293619
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 15 June 2005 |
Time: | 00:30 LT |
Type: | Piper PA-28-181 |
Owner/operator: | Kansas City Aviation Center |
Registration: | N6294C |
MSN: | 28-7890358 |
Year of manufacture: | 1978 |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Raymore, Missouri -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Pinckneyville Du Quoin Airport, IL (KPJY) |
Destination airport: | Olathe-Johnson County Executive Airport, KS (OJC/KOJC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane sustained substantial damage during a forced landing after a loss of engine power. The pilot reported that the projected flight time was "expected to be 2 hours and 36 minutes, and the fuel on board was planned at 5 hours 30 minutes, with a 2 hour reserve." When he was about 25 nm from his destination airport, he started his descent from 4,500 feet mean sea level (msl) to 2,000 feet msl. He reported that he checked the fuel gauges and they indicated that the fuel was "well over half full." When he was about 12 nm from the airport, the engine lost power over a populated area. He executed a forced landing to an area that did not have lights. The airplane landed upright in a muddy field after skidding about 200-300 feet. About one cup of fuel was drained from each wing tank sump and about a spoonful of fuel from the gascolator during the examination of the airplane. There was no evidence of a fuel leak anywhere on the airplane. The engine was rotated and thumb compression was observed on all cylinders, and spark was observed on all spark plugs. The pilot rented the airplane from a fixed base operator on June 10, 2005. The airplane was dispatched with the fuel tanks topped off with 48 gallons of fuel. The pilot reported that he flew nonstop to an airport located 246 nautical miles away. The pilot reported that on June 14, 2005, he flew to an airport that was 23 nautical miles away where he purchased 20.0 gallons of fuel. The pilot then flew back to the same airport 23 nautical miles away before departing on the accident flight later that night. The tachometer indicated the airplane had operated 6.2 hours, and the Hobbs meter indicated the airplane had flown 6.0 hours since the airplane was dispatched to the pilot on June 10th. The Pilot's Operating Handbook (POH) indicated that the average fuel burn at 75 percent power with the engine properly leaned was about 10.5 gallons per hour. The average fuel burn for the accident airplane during the 6.0 hours (Hobbs time) it had been rented to the pilot was about 11.3 gallons per hour.
Probable Cause: The loss of total engine power due to fuel exhaustion as a result of the pilot's inadequate preflight. A factor was the unsuitable terrain encountered during the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI05CA142 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI05CA142
Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 08:18 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation