Accident Piper PA-32R-301T N341MA,
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ASN Wikibase Occurrence # 293699
 
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Date:Sunday 5 June 2005
Time:22:12 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-301T
Owner/operator:David Harlow Pease Iii
Registration: N341MA
MSN: 3257041
Year of manufacture:1998
Total airframe hrs:1032 hours
Engine model:Lycoming TIO-540-AH1A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Tazewell, Tennessee -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Asheville Regional Airport, NC (AVL/KAVL)
Destination airport:Cincinnati Municipal Airport, OH (LUK/KLUK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
At 2130, the pilot informed Indianapolis Center Air Traffic Controller that he was having an emergency. The airplane then lost engine power. The Controller provided information about nearby airports, but the pilot could not locate any of the airports. Another airplane in the vicinity tried to assist in visually locating a nearby airport, but was also unsuccessful. The pilot maneuvered for an emergency landing and the airplane collided with a tree, pickup truck and a mobile home. Examination of the aircraft revealed both wings detached, the propeller and engine cowling separated from the airplane, and the firewall buckled. The nose of the airplane was crushed and all three blades of the propeller were bent. Oil was across the belly of the fuselage and no oil was recovered from the engine. The fuel tanks were breached, but fuel was found in the fuel bowl and the fuel servo. Photographs of the accident scene showed the turbocharger oil drain tank separated from its mount and hanging from the oil scavenge line and oil breather line. The mounting flange remained attached to the turbocharger. The oil return line threads that attached to the oil drain tank were not damaged. The turbine housing at the turbocharger oil drain tank attachment area was discolored. The turbocharger center section oil supply line check valve was field tested by applying 30 inches of air pressure and was functional. The turbocharger teardown revealed no evidence of oil leakage from the turbocharger assembly. The turbocharger was manufactured in March 1988 and was overhauled and reinstalled on the airplane by a repair facility on June 3, 2005, 2 days before the accident. The pilot's kneeboard was recovered. Kneeboard notes dated June 5, 2005, the day of the accident, contained a notation of 'Symptoms,” followed by entries of 'blue smoke” and 'oil puddle.” Additional entries appeared to note engine power loss observations.

Probable Cause: Loss of engine power due to oil starvation; the reason for the oil starvation could not be determined.

Accident investigation:
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Investigating agency: NTSB
Report number: ATL05LA094
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB ATL05LA094

Revision history:

Date/timeContributorUpdates
10-Oct-2022 12:21 ASN Update Bot Added

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