Accident Piper PA-32R-300 N333TG,
ASN logo
ASN Wikibase Occurrence # 293717
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Tuesday 31 May 2005
Time:17:45 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-300
Owner/operator:Ram Air Freight Inc
Registration: N333TG
MSN: 32R-7680320
Year of manufacture:1976
Total airframe hrs:6770 hours
Engine model:Lycoming IO-540
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Fort Myers, Florida -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Fort Myers-Page Field, FL (FMY/KFMY)
Destination airport:Naples Airport, FL (APF/KAPF)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that no abnormalities were noted during a thorough preflight inspection or during the walk around. The takeoff roll and initial climb were uneventful, at about 300 feet above the ground, the top cowling of the engine separated and struck the right side of the windshield and the right side of the horizontal stabilator. The pilot returned to the airport and landed without further incident. The center portion of the top engine cowling was not recovered. The right portion of the top engine cowling separated in-flight but was recovered, and the left portion of the top engine cowling remained attached to its two latch points. Examination of the right portion of the cowling revealed that the forward latch was broken and separated in half. Both the forward and aft latches were bent, twisted aft, and canted aft. Examination of the left portion of the cowling revealed no apparent damage to the latches. The accident airplane had a previous incident on October 22, 2003, in which the top engine cowling separated during climb out and impacted the windshield. The airplane returned to the airport and landed without further incident also. Examination of the maintenance records revealed that following the incident in 2003, the top engine cowling was replaced by a cowling which had accumulated 11,800 flight hours at the time of the replacement. That cowling subsequently had actions performed to it, including two repairs of the fiberglass structure accomplished on July 7, 2004 and September 14, 2004. The latter of these repairs addressed a crack at the forward area of the top cowling.

Probable Cause: Inadequate maintenance and repair of the engine top cowling by company maintenance personnel, resulting in failure and separation of the cowling in flight.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA05LA116
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB MIA05LA116

Revision history:

Date/timeContributorUpdates
10-Oct-2022 12:39 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org