Accident Beechcraft A36 N6742S,
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ASN Wikibase Occurrence # 294106
 
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Date:Thursday 10 February 2005
Time:18:30 LT
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft A36
Owner/operator:John Schwegmann
Registration: N6742S
MSN: E1635
Total airframe hrs:2166 hours
Engine model:Continental IO-520-BB
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Bay St. Louis, Mississippi -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Bay St Louis-Stennis International Airport, MS (KHSA)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot/owner of the airplane heard a low thumping noise during takeoff on several occasions, which he associated with the landing gear. He flew the airplane to an airport to have a mechanic familiar with his airplane troubleshoot the noise. After a visual inspection failed to reveal the problem, a test flight was initiated. The mechanic seated in the rear of the airplane heard the noise, and after flying around for a few minutes, requested a return to the airport. During extension of the landing gear, the 3 green (gear down/locked) lights failed to illuminate. The pilot cycled the gear, but the lights again failed to illuminate. He stated he thought he had heard all the appropriate sounds associated with proper landing gear extension, and elected to continue the landing, without attempting the manual extension of the gear as prescribed in the "Emergency Procedures" section of the pilot's operating handbook. During the landing roll the landing gear collapsed. Postaccident testing of the landing gear was conducted with the airplane on jacks. Tests revealed that the charge on the battery was insufficient to extend the electrically operated landing gear completely. The battery was found to be capable of taking a charge, but further tests revealed no output from the alternator. The alternator's rotor was found to be defective and the electrical brushes excessively worn.

Probable Cause: The pilot's failure to use the manual emergency landing gear extension mechanism during the approach to land, which resulted in the electrically actuated main landing gear collapsing during the landing roll. A factor associated with the accident is an inoperative alternator.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC05LA029
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB ANC05LA029

Revision history:

Date/timeContributorUpdates
10-Oct-2022 17:22 ASN Update Bot Added

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