Accident Piper PA-32-300 N364BW,
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ASN Wikibase Occurrence # 294114
 
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Date:Tuesday 8 February 2005
Time:19:12 LT
Type:Silhouette image of generic PA32 model; specific model in this crash may look slightly different    
Piper PA-32-300
Owner/operator:Race City Aviation
Registration: N364BW
MSN: 32-7240006
Year of manufacture:1971
Total airframe hrs:9061 hours
Engine model:Lycoming IO-540-KIA5
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Concord, North Carolina -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Wilmington-New Hanover County International Airport, NC (ILM/KILM)
Destination airport:Concord Regional Airport, NC (USA/KJQF)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, during a cargo flight to Concord Regional Airport, North Carolina at an attitude of approximately 2000 feet, and 5 miles out from runway 20 the engine began to lose power. The pilot switched from the left main tank to the right main tank to regain engine power. Engine power was regained for a brief moment and then started to decrease again to 1000 rpm. The pilot switched from the right main tank to the auxiliary tip tanks, and noted no increase in engine power. The pilot contacted the Concord Regional Airport tower and informed them that the airplane was "going down." The airplane collided in a rock quarry approximately one mile from the approach end of runway 20. Post accident examination of the airplane revealed the engine was displaced aft. Post-accident examination of Fuel Pump model (RG17980D/M) serial # B-4766-3402 revealed that the fuel pump was repaired in the field during the life of the unit. The unit was shipped new prior to 1989. No record of overhaul or upgrade activity by the manufacturer was noted. No evidence of preventive maintenance was noted. Examination of the unit revealed severe wear to the rotor interface with the drive coupling, rubber seal material worn on rubber journal, severe wear to rotor seal. The inside diameter of the rotor seal was severely oversized, and compromised the sealing capability at the pumps drive end. This location revealed extensive leakage during testing.

Probable Cause: The loss of engine power due to the failure of the fuel pump which resulted in fuel starvation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL05LA049
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB ATL05LA049

History of this aircraft

Other occurrences involving this aircraft
14 September 1989 VH-BLM 0 Orchid Beach, QLD sub
Bounced on landing

Revision history:

Date/timeContributorUpdates
10-Oct-2022 17:28 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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