ASN Wikibase Occurrence # 294127
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Date: | Thursday 3 February 2005 |
Time: | 16:00 LT |
Type: | Cessna 152 |
Owner/operator: | Stick And Rudder Club, Inc. |
Registration: | N68714 |
MSN: | 15285332 |
Year of manufacture: | 1981 |
Total airframe hrs: | 7099 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sturtevant, Wisconsin -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Janesville-Rock County Airport, WI (JVL/KJVL) |
Destination airport: | Waukegan Memorial Airport, IL (UGN/KUGN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane experienced a nose gear collapse during a precautionary landing in a corn field. The student pilot stated that her radios became inoperative during the second leg of the solo cross country flight. She elected to bypass the airport she intended on landing at to return to her home airport. During the flight to her home airport, the pilot noticed that the fuel gauges were indicating empty. She stated the airplane was topped off at her last departure point so she should have had plenty of fuel, but she thought the airplane was possibly leaking fuel so she decided to land at a nearby airport. The pilot stated she lowered the flaps while in the traffic pattern, but she doesn't remember the flaps extending. She stated that as she tried to turn onto final approach, the airplane would not bank and the controls felt sluggish. The pilot stated she knew she was not going to make it to the runway so she located a field in which to land. The pilot stated she reduced the power to idle at which time the stall warning sounded so she lowered the nose of the airplane. She stated the field had a slight rise so she held the airplane off the ground as long as possible. The nose gear contacted snow during the landing and the nose gear collapsed. Post accident inspection of the airplane revealed corrosion was present at the wiring connectors on the master switch. The fuel gauges, radios, and flaps, are electrically actuated components. The flight controls were inspected and control continuity was established.
Probable Cause: The pilot's failure to identify the electrical system failure and to maintain adequate airspeed during the landing approach. Factors associated with the accident were the electrical system failure, the snow covered terrain, and the pilot's lack of experience.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI05LA067 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB CHI05LA067
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 17:35 |
ASN Update Bot |
Added |
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