ASN Wikibase Occurrence # 294134
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Date: | Wednesday 2 February 2005 |
Time: | 15:50 LT |
Type: | Cessna 172N |
Owner/operator: | Patrick Hinton |
Registration: | N618MN |
MSN: | 17269028 |
Total airframe hrs: | 9914 hours |
Engine model: | Lycoming O-320-H2AD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Loveland, Colorado -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | FORT COLLINS, CO (3V5) |
Destination airport: | (3V5) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the flight instructor, they were performing a touch-and-go landing. During the landing flare, the flight instructor requested that the student perform a go-around and the student acknowledged. The instructor stated that the student added full power and "fully and abruptly moved the control yoke to its full forward limit." The instructor stated that he attempted to take control of the airplane; however, the nose gear impacted the runway and the airplane bounced. The instructor stated that he was able to land the airplane, following the bounce. He brought the airplane to a complete stop approximately 15 feet off of the left side of the runway. In two separate telephone interviews, both the flight instructor and the student were asked about the discrepancy between their statements. The flight instructor stated that the accident sequence was as he had stated in his written statement. He felt the student was not remembering approximately 20 seconds of the landing sequence. The student stated that the accident sequence was exactly as he had stated in his written statement. The student also stated that the purpose of the flight was to perform touch-and-go landings, not go-arounds. The student stated that the hard landing was only his third landing. He was unaware of what a go-around procedure was. The airplane was substantially damaged. A postimpact examination of the airplane systems revealed no anomalies.
Probable Cause: The dual student's improper flare and the flight instructor's inadequate supervision.. A contributing factor was the inadequate communication between the flight instructor and the dual student,
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN05LA055 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB DEN05LA055
Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 17:40 |
ASN Update Bot |
Added |
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