ASN Wikibase Occurrence # 294247
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 28 December 2004 |
Time: | 19:26 LT |
Type: | Beechcraft BE35 |
Owner/operator: | Craig Thomas Hughes |
Registration: | N860R |
MSN: | CD-11 |
Total airframe hrs: | 4308 hours |
Engine model: | Teledyne Continental IO-470-J |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Los Fresnos, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Gladewater, TX (07F) |
Destination airport: | Brownsville-South Padre Island International Airport, TX (BRO/KBRO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The 1,172-hour pilot reported that the engine lost power when he increased manifold pressure after he leveled off at an altitude of 1,200 feet while on a night cross country flight. The pilot was able to restart the engine by adjusting the mixture and turning on the fuel boost pump; however, the engine lost power a second time. He then initiated a forced landing to an open field with the landing gear retracted. After the airplane came to rest , the pilot secured the airplane and placed the fuel selector to the "off" position. Examination of the airplane revealed there was no fuel in the auxiliary tanks, 20 gallons in the left main tank, and approximately 15 gallons in the right main fuel tank. The pilot said that he had previously experienced a loss of engine power on three different occasions in this airplane, and was able to restore power. After each of those power losses the airplane was examined by an airframe and power plant mechanic, and no deficiencies were identified. The engine was test-run under the supervision of the Safety Board. The engine started immediately and ran at various power settings without interruption for approximately 30 minutes. No mechanical deficiencies were noted.
Probable Cause: The loss of engine power for undetermined reasons. A contributing factor was the prevailing dark night ilumination.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW05LA049 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB DFW05LA049
Revision history:
Date/time | Contributor | Updates |
11-Oct-2022 04:53 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation