ASN Wikibase Occurrence # 294250
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Date: | Saturday 25 December 2004 |
Time: | 15:45 LT |
Type: | Cessna 150C |
Owner/operator: | |
Registration: | N7857Z |
MSN: | 15059957 |
Year of manufacture: | 1963 |
Total airframe hrs: | 4341 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | East Moriches, New York -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | East Moriches, NY (1N2) |
Destination airport: | East Moriches, NY (1N2) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On departure from the Spadaro Airport (1N2), East Moriches, New York, the airplane's engine experienced a partial loss of power. The pilot attempted to restore full power by using the carburetor heat control, without result. He then performed a forced landing on a road. The airplane bounced, and touched down in a field. During the rollout the airplane struck an obstruction nosed over and was substantially damaged. Examination of the wreckage, revealed that the fuel tanks appeared to be almost full. Fuel was drained from the airplane and no contamination was observed. An examination of the engine was also conducted. Crankshaft and camshaft continuity was confirmed. The magnetos produced spark at all spark plugs. During A differential pressure test, air could be heard to discharge at the oil filler/crankcase breather and cylinders #1 and #3, exhibited readings below the leakage limits. During an internal inspection of the #1 and #3 cylinders, heavy carbon deposits were found on both the cylinder heads and valves. Wear was also visually observed on the cylinder walls and both rod end bearings exhibited excessive play. The airplane had received an annual inspection 55 flight hours prior to the accident and the engine was 164 flight hours short of the recommended overhaul time.
Probable Cause: Several mechanical deficiencies which either independently or collectively resulted in a subsequent loss of engine power. A factor in the accident was the obstruction in the forced landing area.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD05LA026 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB IAD05LA026
Revision history:
Date/time | Contributor | Updates |
11-Oct-2022 04:57 |
ASN Update Bot |
Added |
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