Accident Mooney M20F N3208F,
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ASN Wikibase Occurrence # 294299
 
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Date:Thursday 9 December 2004
Time:16:12 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20F
Owner/operator:
Registration: N3208F
MSN: 670362
Year of manufacture:1967
Total airframe hrs:4000 hours
Engine model:Lycoming IO-360
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Fabens, Texas -   United States of America
Phase: Unknown
Nature:Executive
Departure airport:Fort Stockton-Pecos County Airport, TX (FST/KFST)
Destination airport:El Paso International Airport, TX (ELP/KELP)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The 600-hour private pilot reported that he began "having engine difficulties." The pilot noticed, "the #2 cylinder head temperature gauge was indicating a lower than normal temperature, and shortly thereafter, there was a loss of engine oil pressure." The pilot then determined that there were no available airport landing sites, and few minutes later, the engine stopped. He prepared to execute an off-airfield emergency landing. He determined that the safest place to land was the westbound lane of an interstate highway below him. During the landing flare, the right wing of the airplane collided with the rear of a large semi-tractor truck that was traveling on the highway. The airplane then flipped over and came to rest inverted.
A certificated airframe and powerplant mechanic examined the engine under the supervision of the FAA inspector. The examination revealed that the connecting rod to the # 2 piston was broken. The piston was seized inside of the cylinder and could not be removed. No rod bolts or hardware were found. There was damage to the engine case between the #2 and #4 cylinders. The spark plugs were removed and inspected, and no anomalies were found. The oil filter and oil screen were removed, and metal flakes were observed. Oil was not observed on the dipstick or anywhere in the engine, nor did it appear on the exterior surface of the airplane.

Probable Cause: The loss of engine power as a result of the failure of a connecting rod due to oil starvation/exhaustion. A contributing factor was the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DFW05LA033
Status: Investigation completed
Duration: 1 year 1 month
Download report: Final report

Sources:

NTSB DFW05LA033

Revision history:

Date/timeContributorUpdates
11-Oct-2022 14:56 ASN Update Bot Added

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