ASN Wikibase Occurrence # 294347
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Date: | Friday 19 November 2004 |
Time: | 22:30 LT |
Type: | Beechcraft A36TC |
Owner/operator: | Repro-air, LLC |
Registration: | N38047 |
MSN: | EA-176 |
Year of manufacture: | 1980 |
Engine model: | Teledyne Continental TSIO-520-UB |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Huntsville, Alabama -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | San Antonio International Airport, TX (SAT/KSAT) |
Destination airport: | Huntsville International Airport, AL (HSV/KHSV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight was being vectored for the ILS 18L approach when the pilot reported a loss of engine power approximately 7 miles from the airport at an altitude of approximately 2,000 feet mean sea level (MSL). The pilot stated that he switched main fuel tanks and performed the loss of power procedures as outlined in the Pilot's Operating Handbook, but his attempts to restore engine power were unsuccessful. The pilot performed an off-airport landing with the gear retracted, and the airplane collided with the ground and slid to a stop. The left main fuel tank and left tip tank were empty with no evidence of fuel leakage. Approximately 36 gallons of fuel was recovered from the right main fuel tank, and the right tip tank was empty with no evidence of fuel leakage. The fuel selector handle was positioned to the right tank. Examination of the engine revealed continuity from the cockpit throttle and mixture controls to the fuel servo. The exhaust pipe was crushed. Examination of the top spark plugs revealed no evidence of abnormal wear or deposits. In preparation for a test run, the damaged propeller was removed and a Hartzell three-bladed club prop was installed. A three-inch by three-inch hole was cut in the exhaust pipe above the crushed area to facilitate exhaust flow, and the air inlet was cleared of mud. A portable fuel tank was connected to the supply fitting at the right wing root, and the fuel recovered from the right wing tank was utilized for the test run. An engine start was accomplished utilizing the cockpit controls; the engine started within four to five seconds and was observed to run smoothly. The engine idled smoothly at 700 to 750 rpm, and the engine operated smoothly up to 1900 rpm; higher rpms was not attempted. A magneto check was performed at 1900 rpm, and a drop of 75 rpm was observed for each.
Probable Cause: The pilot's improper fuel management, which resulted in a loss of engine power due to fuel starvation and a forced landing to an open field.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL05CA027 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB ATL05CA027
Revision history:
Date/time | Contributor | Updates |
11-Oct-2022 15:38 |
ASN Update Bot |
Added |
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