ASN Wikibase Occurrence # 294485
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Date: | Saturday 18 September 2004 |
Time: | 12:30 LT |
Type: | Cessna 172M |
Owner/operator: | Private |
Registration: | N80237 |
MSN: | 17266465 |
Year of manufacture: | 1975 |
Total airframe hrs: | 6244 hours |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Houstonia, Missouri -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Lee's Summit Municipal Airport, MO (KLXT) |
Destination airport: | Columbia Regional Airport, MO (COU/KCOU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane sustained impact and fire damage when it cart-wheeled during a forced landing following a loss of engine power. The pilot reported that 30 minutes into the flight he heard a "clunk", the engine stopped running, and the propeller was not windmilling. He stated he attempted to restart the engine to no avail. The pilot was attempting an off airport landing in a bean field when the right wing contacted the ground, the airplane cart wheeled, and a post impact fire ensued. Inspection of the engine revealed the piston and piston pin on the number 4 cylinder were separated from the connecting rod. The metallurgical examination of the number 4 connecting rod noted the piston pin end of the rod was fractured and the fractured ends were deformed inward. The fractured surface revealed an area typical of a fatigue crack that started at the forging parting plane on the exterior surface. The fatigue origin areas contained ratchet marks indicating that fatigue cracking initiated at multiple sites and the crack extended through approximately 60% of the wall thickness. The engine, a Lycoming O-320-E2D, was overhauled on August 11, 2003, at an engine total time of 3,918.7 hours. The engine had accumulated approximately 70 hours since the overhaul. Maintenance records indicate the connecting rods were magnafluxed, rebushed, checked for alignment, and reinstalled in the engine during the overhaul. The connecting rods were the original engine rods.
Probable Cause: The fatigue failure of the piston end of the connecting rod and the pilot's failure to maintain aircraft control during the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI04LA283 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB CHI04LA283
Revision history:
Date/time | Contributor | Updates |
11-Oct-2022 18:46 |
ASN Update Bot |
Added |
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