Accident Mooney M20F N9708M,
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ASN Wikibase Occurrence # 294546
 
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Date:Sunday 5 September 2004
Time:14:32 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20F
Owner/operator:
Registration: N9708M
MSN: 670268
Year of manufacture:1967
Total airframe hrs:4020 hours
Engine model:Lycoming I0-360-A1A
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Brandon, Mississippi -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Atlanta-DeKalb Peachtree Airport, GA (PDK/KPDK)
Destination airport:Shreveport Downtown Airport, LA (DTN/KDTN)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that he performed a preflight inspection of the airplane and noted the oil capacity was full (8 quarts). Approximately 2 hours into the flight while flying at 10,500 feet, the engine began running rough. He advised air traffic control (ATC), and attempts to correct the rough running engine were unsuccessful. The flight continued and shortly afterwards, the engine developed a severe roughness and he then heard a bang with smoke entering the cockpit. He declared "mayday" with ATC, and requested vectors to the nearest airport. Unable to land there, he executed a forced landing on a nearby highway and collided with a vehicle during the landing roll-out. The No. 3 cylinder was found separated from the crankcase, and all cylinder studs and/or thru-bolts exhibited various forms of fatigue. The No. 3 cylinder connecting rod bolts which were fractured exhibited evidence of either bending or shear overstress. The No. 2 cylinder connecting rod bearing was found welded to the crankpin, and a piece of aluminum lined bearing material was found inside the oil passage of the No. 2 cylinder crankpin journal. Fretting was noted at the No. 3 cylinder contact area, and also at the split-line surface of the right crankcase half at the main bearing locations. The fretting was the greatest at the cylinder contact area between studs Nos. 1 and 2, and also at the split line surface on the right crankcase half at the No. 3 main bearing location. The engine had accumulated 1,390 hours since major overhaul and approximately 873 hours since the No. 3 cylinder was removed and reinstalled.

Probable Cause: A loss of engine power due to the fatigue failure of all studs and/or thru-bolts of the No. 3 cylinder for undetermined reasons causing separation of the cylinder. Contributing to the accident was the unsuitable terrain encountered by the pilot.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA04LA127
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB MIA04LA127

Revision history:

Date/timeContributorUpdates
11-Oct-2022 19:28 ASN Update Bot Added

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