ASN Wikibase Occurrence # 294621
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Date: | Saturday 21 August 2004 |
Time: | 13:30 LT |
Type: | Fall Cub |
Owner/operator: | Martin Kenric Fall |
Registration: | N25MF |
MSN: | 5 |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Rockville, Indiana -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | INDIANAPOLIS, IN (7L8) |
Destination airport: | Rockville, IN |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The experimental amateur-built airplane sustained substantial damage on impact with terrain during a forced landing at a private airstrip following an in-flight loss of engine power. The pilot and passenger were hospitalized with serious injuries. The pilot's accident report stated, "I flew a 3-4 hundred foot pass down runway (W to E) at a fairly low power setting to assess the strip and its condition. As I started a [right hand] turn to go west so that I could go back to land east, the engine quit (it windmilled). ... I turned sharply west to at least land in cornfield [and] possibly runway. ... [The airplane] was settling, however and [left] gear drug thru top of 75' tree slowing me considerably. [The airplane] hit corn slightly nose down in flat attitude." Concerning the loss of engine power, the pilot stated, "Engine quit - fuel starvation, I feel caused by unporting fuel pickups." The pilot's safety recommendation was, "Fuel system need to be reevaluated, possibly rerouting fuel lines from tanks, adding a fuel pump (gravity fed) and/or more fuel pickup points. [Approximately] 12 gal. of fuel showed on fuel sight [glasses] at time engine quit."
Probable Cause: The fuel starvation encountered due to the builder's inadequate fuel system design and the subsequent loss of engine power during a maneuver for the landing approach. Factors were the tree and corn.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI04LA245 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB CHI04LA245
Revision history:
Date/time | Contributor | Updates |
12-Oct-2022 07:04 |
ASN Update Bot |
Added |
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