Accident American Aviation AA-1A Trainer N9442L,
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ASN Wikibase Occurrence # 294692
 
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Date:Friday 6 August 2004
Time:09:30 LT
Type:Silhouette image of generic AA1 model; specific model in this crash may look slightly different    
American Aviation AA-1A Trainer
Owner/operator:
Registration: N9442L
MSN: AA1A-0242
Year of manufacture:1971
Engine model:Lycoming O-320-E2D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Eudora, Kansas -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Olathe-New Century AirCenter, KS (JCI/KIXD)
Destination airport:Olathe-New Century AirCenter, KS (JCI/KIXD)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was substantially damaged during a forced landing following a loss of engine power. The pilot reported that they were returning after an approximately 30 minute local flight when the engine began to run rough. The airplane was established in a descent and the pilot leveled off at 1,200 feet above ground level. He stated that he moved the mixture control to full rich, however, the engine quit completely. The pilot stated he saw an open field to his right and set-up for a forced landing. He reported that due to the low altitude, he did not switch fuel tanks or attempt to determine the cause of the loss of engine power. The pilot stated the airplane touched down in the field on the main landing gear. He attempted to hold the nose wheel off the ground as long as possible, however, when it dropped the airplane nosed over. The airplane came to rest inverted. A post-accident examination was conducted. Fuel was leaking out of the left tank cap and when the cap was loosened fuel began pouring out of the tank. The right fuel tank cap was secure and when removed, the tank appeared to be empty. No evidence of fuel on the ground was observed at the accident site. The cockpit fuel selector was set to the right tank. Inspection of the fuel system did not reveal any anomalies. No debris was observed in samples taken from the system.

Probable Cause: A loss of engine power due to fuel starvation resulting from the pilot's selection of a fuel tank with an insufficient quantity remaining.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI04LA238
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB CHI04LA238

Revision history:

Date/timeContributorUpdates
12-Oct-2022 08:01 ASN Update Bot Added

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