Accident Mooney M20J N91381,
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ASN Wikibase Occurrence # 294735
 
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Date:Wednesday 28 July 2004
Time:14:03 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20J
Owner/operator:Private
Registration: N91381
MSN: 24-3237
Year of manufacture:1991
Total airframe hrs:6328 hours
Engine model:Lycoming IO-360
Fatalities:Fatalities: / Occupants: 3
Aircraft damage: Destroyed
Category:Accident
Location:Fox Lake, Illinois -   United States of America
Phase: Unknown
Nature:Training
Departure airport:Chicago-Executive Airport, IL (PWK/KPWK)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was destroyed when it impacted a road following an uncontrolled descent. Examination of the airplane revealed no anomalies existed prior to impact. The pilot seated in the left seat had recently purchased the airplane. The pilot seated in the right seat was a certified flight instructor. According to the CFI's logbook, he had 2,401.4 hours total flight experience and 62.6 hours experience as a flight instructor. Radar track data showed the aircraft departed Palwaukee Airport, Wheeling, Illinois, and proceeded toward Fox Lake, Illinois. The last recorded radar return coincided with the time and location of the accident site. The radar data showed that during the 3 minutes prior to the last return, the airplane's groundspeed slowed from 158 knots to 70 knots while the altitude returns remained between 2,300 and 2,500 feet. The last two radar returns show the airplane descending through 2,200 feet and 1,700 feet pressure altitudes, respectively. The calculated ground speed during these last two radar returns was 63 knots and 42 knots, respectively. The Pilot's Operating Handbook for the airplane lists stall speeds with 0-degree bank angle between 48.5 knots and 59 knots calibrated airspeed (CAS) depending on weight and configuration. The gear-up, flaps-up stall speed at 2,300 pounds and 0-degree bank angle was listed at 54 knots CAS. The gear-down, flaps 33-degree stall speed for the same weight and bank angle was listed as 48.5 knots CAS.

Probable Cause: The flight crew's failure to maintain airspeed which led to an inadvertent stall/spin. An additional cause was the flight instructor's unsuccessful remedial action during the course of the accident sequence. The slow flight performed was a factor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI04FA198
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB CHI04FA198

History of this aircraft

Other occurrences involving this aircraft
25 July 1998 N91381 Private 0 Alexander City, AL sub

Revision history:

Date/timeContributorUpdates
12-Oct-2022 08:30 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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