ASN Wikibase Occurrence # 294756
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 23 July 2004 |
Time: | 20:03 LT |
Type: | Cessna 172RG |
Owner/operator: | San Diego Flight Training Int'l Inc. |
Registration: | N5167R |
MSN: | 172RG0043 |
Year of manufacture: | 1979 |
Total airframe hrs: | 7218 hours |
Engine model: | Lycoming O-360-F1A6 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Diego, California -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | San Diego-Montgomery-Gibbs Executive Airport, CA (MYF/KMYF) |
Destination airport: | San Diego-Montgomery-Gibbs Executive Airport, CA (MYF/KMYF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The right main landing gear collapsed during rollout following a normal touchdown on the runway. Thereafter, directional control was lost, and the right wing struck the surface of the runway. The airplane veered off the runway, and it came to rest in an adjacent open dirt field. During flight the pilot had experienced a low voltage condition, and his radio communications became problematic as the battery gradually discharged. The pilot cycled the airplane's master electric system switch in accordance with instructions in the Cessna Pilot's Operator's Handbook. Because this did not restore electric power, the pilot reduced the electrical load to conserve energy. No evidence of any mechanical malfunction was found during the post impact examination of the landing gear and alternator/battery electric system. During the examination the alternator field circuit breaker was found in the tripped position. The examination revealed that when the alternator circuit breaker was reset, electric current was restored to the buss and the battery was charging. Prior to landing, the pilot failed to properly perform procedures relating to ensuring that the alternator circuit breaker was engaged. Also, the pilot failed to ensure that the landing gear was fully extended by using the emergency gear extension system.
Probable Cause: The pilot's failure to ensure that the landing gear was fully extended, by use of the emergency gear extension system, which resulted in its partial collapse during landing rollout. Also causal was the pilot's failure to follow POH procedures relating to troubleshooting and restoring electric power to the airplane busses.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX04LA277 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB LAX04LA277
History of this aircraft
Other occurrences involving this aircraft
28 December 2014 |
N5167R |
American Aviation Academy Inc |
0 |
Gillespie Field Airport (KSEE), San Diego/El Cajon, CA |
|
min |
Gear-up landing |
Revision history:
Date/time | Contributor | Updates |
12-Oct-2022 08:42 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation