ASN Wikibase Occurrence # 294892
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Date: | Saturday 27 December 2003 |
Time: | 15:42 LT |
Type: | Cirrus SR22 |
Owner/operator: | Alex Mesa |
Registration: | N742CD |
MSN: | 0139 |
Year of manufacture: | 2002 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | King, North Carolina -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Martinsville-Blue Ridge Airport, VA (KMTV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated he was at 5,500 feet explaining to a passenger what he would do in the event of an engine failure. He pulled the power back, continued the explanation, and turned towards a forced landing area. He increased throttle at 3,500 feet in order to change his direction and head back. The power lever felt funny and the engine did not respond. He continued to monitor his instruments and continued with the forced landing. He did not inform his passengers of the emergency. The pilot did not remember seeing the power lines before the collision. The front seat passenger informed the Highway Patrol Officer who responded to the accident site that when the pilot attempted to climb out from the approach, the airplane collided with the power line and the ground. A witness on the ground who observed the accident stated the airplane was in a right descending turn heading towards an open field. Examination of the airframe, flight controls, and throttle assembly, revealed no anomalies. The engine was mounted in a test stand. The engine started and ran at idle power. After engine warm up the throttle was increased to 2,000 rpm and a magneto check was completed. The throttle was advanced to full power and back to the idle position. The engine was shut down with the mixture control..
Probable Cause: A loss of engine power for undetermined reasons and the pilot's failure to maintain a visual lookout and obstacle clearance while performing a simulated engine out resulting in an in-flight-collision with a power line and the ground.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB ATL04LA060
Revision history:
Date/time | Contributor | Updates |
12-Oct-2022 15:28 |
ASN Update Bot |
Added |
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