ASN Wikibase Occurrence # 294909
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Date: | Sunday 21 December 2003 |
Time: | 13:00 LT |
Type: | Cessna 310P |
Owner/operator: | Crystal Aero Group Inc., |
Registration: | N5811M |
MSN: | 310PO111 |
Total airframe hrs: | 5504 hours |
Engine model: | Continental IO-470-VO |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Crystal River, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Crystal River Airport, FL (KCGC) |
Destination airport: | Crystal River Airport, FL (KCGC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that during takeoff/initial climb, at an altitude of about 500 feet, he placed the landing gear handle in the "UP" position, and during retraction, heard a loud bang, and the rudder pedals shuttered. He said he lowered the gear handle, and received a green light indication only the main gear. He then retarded the throttle levers to check for the landing gear warning horn, but the horn did not activate. He said he then performed the emergency gear extension procedure, but the nose gear did not extend. During subsequent landing rollout, as the airspeed decreased the nose gear collapsed, and the airplane skidded to a halt on the runway. Examination of the airplane's maintenance records showed that maintenance had been performed on the airplane's nose gear 11 hours prior to the accident, and 5 hours prior to the accident the airplane had received an annual inspection. Postaccident examination of the airplane's nose landing gear revealed that the damage was consistent with the nose gear strut not receiving proper service, having deflated, and being out of alignment.
Probable Cause: Inadequate maintenance by company maintenance personnel, which resulted in operation of the airplane with a deflated nose landing gear strut, which resulted in the nose gear failing to lock in position, gear collapse, and damage to the airplane during landing rollout.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA04LA036 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB MIA04LA036
Revision history:
Date/time | Contributor | Updates |
12-Oct-2022 15:40 |
ASN Update Bot |
Added |
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