ASN Wikibase Occurrence # 294957
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Date: | Sunday 30 November 2003 |
Time: | 11:35 LT |
Type: | Cessna T210K |
Owner/operator: | Private |
Registration: | N81PC |
MSN: | T210K59381 |
Total airframe hrs: | 5320 hours |
Engine model: | Continental TSIO520R |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Deming, New Mexico -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Oakland International Airport, CA (OAK/KOAK) |
Destination airport: | Deming Airport, NM (DMN/KDMN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on approach to the airport. At 5 nautical miles from the airport, the airplane was approximately 4,000 feet above ground level. The pilot lowered the landing gear, set 30 degrees of flaps, and initiated several "S" turns to lose altitude. The pilot said that at 2 miles from the runway, he switched his fuel selector to the right fuel tank, which had more fuel. The pilot continued the "S" turns until he was 1/3 mile from the end of the runway. When he applied power to level off, there was no response. The pilot selected a field to the right of his final approach course. The airplane touched down approximately 20 feet short of his intended field. The airplane struck a wrought iron fence, collapsing the nose gear and the left main landing gear. An examination of the engine showed no evidence of fuel in the fuel distribution manifold or fuel lines. An examination of the fuel tanks showed some fuel in the right fuel tank. An examination of the airplane's, engine controls and remaining systems revealed no anomalies.
Probable Cause: The pilot's improper in-flight planning and decision. Factors contributing to the accident were fuel exhaustion and the fence.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN04LA025 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB DEN04LA025
Revision history:
Date/time | Contributor | Updates |
12-Oct-2022 16:15 |
ASN Update Bot |
Added |
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