ASN Wikibase Occurrence # 295107
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Date: | Sunday 12 October 2003 |
Time: | 14:00 LT |
Type: | Fairchild 42 |
Owner/operator: | |
Registration: | N106M |
MSN: | 4 |
Total airframe hrs: | 1801 hours |
Engine model: | Pratt & Whitney R985-14B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wasilla, Alaska -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Wasilla, AK (0AK1) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The accident pilot, a certified aircraft mechanic, reported the airplane was in cruise flight when the engine had a total loss of engine power. Emergency procedures failed to restart the engine, and the pilot selected an airstrip for an emergency landing site. The airplane was unable to reach the airstrip, and collided with trees. Postaccident inspection of the engine disclosed a leaking carburetor. The leaking carburetor was removed, and replaced with a serviceable carburetor. The engine started and ran without any observed deficiencies. The leaking carburetor was disassembled, and the metal float was found to be cracked. The metal float contained 2.4 ounces of fuel. The pilot noted that he had recently purchased the carburetor from an aircraft mechanic, and that he had requested the carburetor to be overhauled prior to installation on the accident airplane. The mechanic stated he did not perform the carburetor float leak check because he only de-preserved the carburetor, and did not overhaul the carburetor. The carburetor had been installed on the airplane about 3 flight hours prior to the accident.
Probable Cause: The inadequate inspection of the carburetor by the aircraft mechanic who had recently worked on the carburetor, which failed to detect a cracked float, resulting in a total loss of engine power during cruise flight. A factor associated with the accident was the lack of suitable terrain for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC04LA003 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB ANC04LA003
Revision history:
Date/time | Contributor | Updates |
12-Oct-2022 18:02 |
ASN Update Bot |
Added |
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