Accident Mooney M20J N201DV,
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ASN Wikibase Occurrence # 295583
 
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Date:Friday 4 July 2003
Time:10:18 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20J
Owner/operator:Private
Registration: N201DV
MSN: 24-0088
Year of manufacture:1977
Total airframe hrs:2263 hours
Engine model:Lycoming IO-360
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Renton, Washington -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Renton Airport, WA (RNT/KRNT)
Destination airport:Renton Airport, WA (RNT/KRNT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that the airplane experienced an electrical malfunction 2-3 minutes after takeoff. After multiple unsuccessful attempts to reset the electrical system, the pilot attempted to manually lower the landing gear in preparation for a landing. He reported that he was able to actuate the manual gear extension handle, however, the landing gear would not fully extend and lock. After multiple additional attempts to fully lower the gear, the pilot initiated a landing with the main landing gear in the midrange position. Examination of the landing gear system by representatives from the NTSB and FAA revealed that the landing gear actuator housing fractured, and separated from the gearbox. Damage was also noted to the actuator drive coupling. Representatives from the FAA and the manufacturer of the gear assembly conducted the teardown and examination of the electric landing gear actuator motor. During the examination, 14 volts was applied to the actuator motor in an attempt to functionally test the DC motor. The electric motor did not respond, or draw current. Further examination of the motor revealed that the two brushes in the motor were of dissimilar type and design and showed signs of arcing. Additionally, the motors armature showed signs of severe wear. Logbook records indicated that the electric landing gear motor was serviced on February 1, 2001, approximately 39 flight hours prior to the accident. The log entry indicated that the armature shaft and brushes were replaced and that the gear motor was returned to service.


Probable Cause: In-flight failure of the electric landing gear motor during the initial takeoff climb.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA03LA128
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB SEA03LA128

Revision history:

Date/timeContributorUpdates
13-Oct-2022 10:13 ASN Update Bot Added

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