ASN Wikibase Occurrence # 295643
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Date: | Wednesday 25 June 2003 |
Time: | 12:55 LT |
Type: | Cessna 172M |
Owner/operator: | Private |
Registration: | N20679 |
MSN: | 20679 |
Total airframe hrs: | 3300 hours |
Engine model: | Lycoming O-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bristow, Oklahoma -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Branson/Point Lookout-M Graham Clark Airport, MO (PLK/KPLK) |
Destination airport: | Bristow, OK (3F7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While en route to Oklahoma City, the pilot decided to permit a pilot-rated passenger to practice touch-and go landings at Jones Memorial Airport, Oklahoma. The pilot-rated passenger, who was manipulating the controls and occupying the left seat, flared high and the airplane bounced twice. On the second bounce, the airplane veered across the runway. The pilot, who was in the right seat, announced that he was taking over the controls of the airplane to initiate a go-round. During the go-around, the pilot turned the airplane left, applied full power, and lifted the flap lever intending to take out 10 degrees of the 40 degrees that was set for landing. However, the pilot inadvertently took out more than 10 degrees. The airplane drifted left of the runway and descended until the right wing tip struck the ground. The pilot made a correction to the left, but the airplane stalled and pivoted nearly 180 degrees before coming to rest approximately 100 yards east of the runway. The pilot reported the wind to be from 120 degrees at 7-10 knots, and the investigator calculated the density altitude to be 3,278 feet at the time of the accident. Examination of the wreckage indicated from the position of the flap-actuator that the flaps were in the retracted position.
Probable Cause: The pilot's premature retracting of the flaps, and his failure to maintain airspeed which resulted in an inadvertent stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW03LA177 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB FTW03LA177
Revision history:
Date/time | Contributor | Updates |
13-Oct-2022 11:00 |
ASN Update Bot |
Added |
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