Accident Republic RC-3 Seabee N6723K,
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ASN Wikibase Occurrence # 295688
 
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Date:Monday 16 June 2003
Time:17:30 LT
Type:Silhouette image of generic RC3 model; specific model in this crash may look slightly different    
Republic RC-3 Seabee
Owner/operator:Private
Registration: N6723K
MSN: 1006
Total airframe hrs:1851 hours
Engine model:Lycoming GO-435-C2B2
Fatalities:Fatalities: / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Yelm, Washington -   United States of America
Phase: Unknown
Nature:Ferry/positioning
Departure airport:Yelm, WA (92W)
Destination airport:Kent, WA (S36)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Prior to the flight the pilot-rated passenger and first pilot discussed who would operate the aircraft. The passenger would occupy the left seat and taxi the airplane to the active runway, while the first pilot would occupy the right seat and do the flying. The passenger did not remember if the parking brake was set or released prior to beginning his taxi, but did remember that the aircraft did not pull to the left or right while taxiing. Upon reaching the active runway and getting the airplane lined up, the first pilot took control of the airplane and advanced the throttle. The passenger said he didn't feel like the airplane was accelerating properly, and when he asked the first pilot if the airplane was accelerating properly, the first pilot replied, "Yes." As the airplane continued down the runway on its takeoff roll, and sensing the airplane was still not accelerating, the passenger asked the first pilot if he wanted him to put some flaps on. The first pilot replied, "No," and there were no further communications between the passenger and first pilot. The airplane continued off the end of the runway and through a 66 foot grass overrun before going over an embankment and impacting trees. The aircraft subsequently came to rest inverted at the bottom of a ravine. The fuselage and tail section of the aircraft were oriented up and parallel to the slope of the ravine, while the nose and left wing of the aircraft were partially submerged in the adjacent canal which borders the edge of the ravine. Witnesses to the accident thought the pilot was doing a high speed taxi, that the airplane reached a maximum speed of approximately 50 miles per hour, and that there was no attempt to abort the takeoff roll. Several witnesses reported that the engine didn't sound right, was making noises, and was not running smoothly. A post accident examination of the airframe, engine, and propeller did not reveal any anomalies which would have precluded normal operation of the aircraft.

Probable Cause: The failure of the pilot to abort the takeoff roll. Factors contributing to the accident included the failure of the aircraft to accelerate for undetermined reasons and the trees.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA03FA106
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB SEA03FA106

Revision history:

Date/timeContributorUpdates
13-Oct-2022 11:30 ASN Update Bot Added

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