Fuel exhaustion Accident RotorWay Exec 162F N92AL,
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ASN Wikibase Occurrence # 296076
 
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Date:Thursday 27 March 2003
Time:18:00 LT
Type:Silhouette image of generic EXEC model; specific model in this crash may look slightly different    
RotorWay Exec 162F
Owner/operator:Private
Registration: N92AL
MSN: 6619
Total airframe hrs:16 hours
Engine model:Rotorway 6444-162F
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Greensboro, North Carolina -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Greensboro/High Point-Piedmont Triad International Airport, NC (GSO/KGSO)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, he flew around the airstrip for approximately 45 minutes. After several passes over the airstrip, the pilot reported he received an electronic control unit (ECU) failure indication light. When the engine lost power, the pilot entered an autorotation. During the touchdown phase of the autorotation, the helicopter rolled over on the left side. During the examination of the helicopter no fuel was found in the fuel tanks or at the accident site. The ECU's were sent to be bench tested. The test revealed, the last 30 seconds of the flight indicated an increase in the throttle position with a corresponding decrease of engine RPM, with a rapid cycling during the final 12 seconds prior to the engine completely shutting down. The data retrieved from the ECUs revealed the flight prior to the accident lasted 10 minutes with a three-minute ground run. The accident flight was approximately 57 minutes. The pilot stated that the helicopter fuel tank capacity is 14 gallons, and can fly for 2 hours or 180 miles with full fuel. According to the pilot, the helicopter departed with 14 gallons of automotive fuel.









Probable Cause: The pilot's inadequate preflight planning of fuel required for flight which resulted in fuel exhaustion, and a complete loss of engine power followed by a forced landing, and a dynamic rollover during the autorotative touchdown.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL03LA072
Status: Investigation completed
Duration: 2 years
Download report: Final report

Sources:

NTSB ATL03LA072

Revision history:

Date/timeContributorUpdates
13-Oct-2022 16:18 ASN Update Bot Added

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