Accident Cessna FA150K N922SZ,
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ASN Wikibase Occurrence # 296100
 
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Date:Sunday 23 March 2003
Time:11:00 LT
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna FA150K
Owner/operator:Private
Registration: N922SZ
MSN: 0047
Year of manufacture:1970
Total airframe hrs:5266 hours
Engine model:Continental O-200-A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Houston, Texas -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Houston-Weiser Air Park, TX (KEYQ)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While recovering from a steep spiral from 3,000 feet msl to 1,000 feet msl, the pilot felt a shudder in the yoke. Utilizing power adjustments, the 496-hour pilot landed the airplane without further incident. Examination of the airplane revealed that the trim tab and hinge had separated from the right elevator. The right stabilizer was bent upward, the trim tab actuator was found loose in the mount, the rivet holes where the trim tab attached to the elevator, were deformed. Examination of the trim tab actuator revealed black electrical tape wrapped around the trim tab actuator body in the area under each clamp. The trim tab was not found. The rivet holes on the elevator exhibited deformation consistent with the trim tab separation pulling the rivet heads through the elevator skin. The part numbers for the trim tab actuator and clamps (AN742D13) were consistent with manufacturers part numbers. When the clamps were closed and the inside diameter measured, one clamp measured .842 inch and the other measured .860 inch in diameter. The Air Force -Aeronautical Standard for the AN742D13 clamp indicated the diameter to be .813 inch. The investigation was not able to determine when the electrical tape was placed on the actuator. The last annual inspection was performed on November 5, 2002, at accumulated aircraft time of 7,708.04 hours.

Probable Cause: The in-flight separation of the elevator trim tab.

Accident investigation:
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Investigating agency: NTSB
Report number: FTW03LA115
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB FTW03LA115

History of this aircraft

Other occurrences involving this aircraft
13 June 1993 N922SZ Private 0 Willis, TX sub

Revision history:

Date/timeContributorUpdates
13-Oct-2022 16:35 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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