Accident Aero Commander 100 N4123X,
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ASN Wikibase Occurrence # 296106
 
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Date:Friday 21 March 2003
Time:16:30 LT
Type:Silhouette image of generic VO10 model; specific model in this crash may look slightly different    
Aero Commander 100
Owner/operator:Private
Registration: N4123X
MSN: 222
Total airframe hrs:2023 hours
Engine model:Lycoming O-320-A2B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:North Pole, Alaska -   United States of America
Phase: Unknown
Nature:Training
Departure airport:North Pole , AK (95Z)
Destination airport:North Pole , AK (95Z)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor was providing primary flight instruction to the student pilot in a wheel-equipped airplane. The instructor pilot reported that just after takeoff from runway 15, about 100 feet above the runway, the airplane's engine began to run rough and lose power, and emergency engine procedures did not restore engine power. The airplane subsequently collided with a stand of trees at the departure end of the runway, and sustained substantial damage to the wings, fuselage, and empennage. An FAA inspector who inspected the airplane reported finding no preaccident mechanical anomalies. The student pilot reported to the FAA inspector that prior to the accident takeoff, just after starting the airplane's engine, the instructor pilot leaned the fuel mixture and applied full carburetor heat during the 15 to 20 minute engine warm-up time. He said that after the engine was warm, they taxied to the departure end of the runway, and started their takeoff roll, with the mixture control and carburetor heat in the same position. He reported that just after takeoff the engine began to run rough, and lose power. He added that the instructor pilot then took control of the airplane, pushed in the carburetor heat control (off), and all engine power was lost. The student pilot reported that immediately following the accident, both pilots noticed that the mixture control was still in the lean position.







Probable Cause: The flight instructor's improper usage of the airplane's fuel mixture control, resulting in a loss of engine power during takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC03LA035
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB ANC03LA035

Revision history:

Date/timeContributorUpdates
13-Oct-2022 16:36 ASN Update Bot Added

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