Accident RotorWay Exec 162F N241WC,
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ASN Wikibase Occurrence # 296196
 
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Date:Saturday 15 February 2003
Time:16:10 LT
Type:Silhouette image of generic EXEC model; specific model in this crash may look slightly different    
RotorWay Exec 162F
Owner/operator:Private
Registration: N241WC
MSN: 6588
Total airframe hrs:172 hours
Engine model:Lycoming IO-320
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Westford, Massachusetts -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Bedford-Hanscom Field, MA (BED/KBED)
Destination airport:Westford, MA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot had just made a steep approach to a confined area and was pulling into a full hover, when the helicopter began a rapid rotation to the left. The pilot applied full right pedal, but could not stop the rotation. He did not perform an autorotation from a hover because he was concerned of landing hard, rolling over, and shedding parts that could have possibly hurt his friend, who was standing nearby. Instead, he lifted the helicopter back up and tried to fly to a vacant area. During the ascent, the pilot was able to slow the rotation by reducing power, but was never able to completely stop the rotation. He was not able to perform an autorotation because he had no forward airspeed, so he put the helicopter down into trees. The pilot stated that he had experienced Loss of Tail Rotor Effectiveness (LTE) in the past, but due to the strong head wind, and the sudden rapidness of the rotation, he did not feel that this was an LTE situation. An FAA inspector reported that one of the tail rotor pitch change links was fractured, but did not take possession of the link at that time. The pilot/owner initially agreed to send the pitch change link to the Safety Board to be examined, but later determined that the part had failed during impact, and discarded the wreckage.

Probable Cause: The inflight loss of control due to the loss of tail rotor effectiveness.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: IAD03LA033
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB IAD03LA033

Revision history:

Date/timeContributorUpdates
13-Oct-2022 17:41 ASN Update Bot Added

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