Accident Cessna 210 N6572X,
ASN logo
ASN Wikibase Occurrence # 296258
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Thursday 23 January 2003
Time:20:01 LT
Type:Silhouette image of generic C210 model; specific model in this crash may look slightly different    
Cessna 210
Owner/operator:Private
Registration: N6572X
MSN: 57572
Total airframe hrs:2591 hours
Engine model:Continental IO-470
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Clarence, Iowa -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Kirksville Municipal Airport, MO (IRK/KIRK)
Destination airport:Waupaca Municipal Airport, WI (KPCZ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot made a gear-up off airport landing following a loss of engine power. The pilot reported he added a quart of oil and strained the fuel tanks prior to the flight. He reported that during the flight while passing through 4,700 feet on his way up to 5,500 feet, the engine started sputtering and shaking. The pilot reported he switched fuel tanks, and adjusted the mixture, propeller control, and throttle. He stated the manifold pressure was indicating the high 20's and he was not sure if the engine was running. He reported the airplane was now at 3,700 feet and descending about 1,000 feet per minute. According to his global positioning system (GPS) the nearest airport was 9.8 miles away. After considering his landing options, the pilot elected to land in an area that was a "big black nothing." The pilot reported that he lowered the landing gear, but it did not engage in the down and locked position. He stated he was going to use the emergency extension hand pump, but he was getting low and decided to concentrate on flying the airplane. The forced landing was made in a harvested cornfield and the airplane contacted a barbwire fence prior to coming to a stop. The engine, a Continental IO-470-E, serial number 77543-O-E, had 1259.28 total hours when it was overhauled on June 30, 1971. The last logbook entry that listed a time since major overhaul (SMOH) for the engine was dated October 29, 2002. The time SMOH listed was 1237 hours. Total time on the airplane at the time of the accident was 2591.69 hours. Post accident inspection revealed it was difficult to turn the propeller by hand. There was a large amount of oil on the bottom of the engine cowling and no oil was found on the dipstick. The source of the oil leak was not determined. Further inspection revealed the crankshaft was broken between the number 2 and number 3 cylinders.

Probable Cause: A failure of the crankshaft for undetermined reasons. Factors associated with the accident were the rough terrain on which the forced landing was made and the night conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI03LA059
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB CHI03LA059

Revision history:

Date/timeContributorUpdates
13-Oct-2022 18:28 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org