ASN Wikibase Occurrence # 296371
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Date: | Monday 2 December 2002 |
Time: | 19:30 LT |
Type: | Cessna 150H |
Owner/operator: | Karl Hoyer |
Registration: | N50346 |
MSN: | 15069243 |
Total airframe hrs: | 5800 hours |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Twentynine Palm, California -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Twentynine Palm, CA (TNP |
Destination airport: | Twentynine Palms Airport, CA (TNP/KTNP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane experienced a loss of engine power in the takeoff initial climb and impacted terrain during a forced landing. After completing two uneventful landings, the student pilot input full throttle and began the third takeoff of the day. Over halfway down the runway, about 75 feet above ground level, the student told the CFI that he did not think the engine was developing full power. The CFI took over the controls and confirmed that the partial power condition. While attempting a soft field landing, the nose landing gear impacted a bush and the airplane nosed over. Temperatures were obtained from a weather reporting station located 14 miles west-northwest of the airport. At 1855, the temperature was 52 degrees Fahrenheit and the dew point was 32 degrees Fahrenheit. At 2000, the temperature was 48 degrees Fahrenheit and the dew point was 32 degrees Fahrenheit. The temperatures and dew points were applied to an industry standard Carburetor Icing Probability Chart, and both were within the "serious icing at glide power" portion of the chart.
Probable Cause: The improper use of carburetor heat, and the instructor's inadequate supervision which resulted in a loss of engine power due to carburetor icing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX03LA044 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB LAX03LA044
Revision history:
Date/time | Contributor | Updates |
13-Oct-2022 19:46 |
ASN Update Bot |
Added |
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