ASN Wikibase Occurrence # 296396
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Date: | Wednesday 27 November 2002 |
Time: | 15:40 LT |
Type: | Piper PA-28-180 |
Owner/operator: | Kevin Lebaron |
Registration: | N9020J |
MSN: | 28-3048 |
Year of manufacture: | 1966 |
Total airframe hrs: | 8096 hours |
Engine model: | Lycoming O-360-A3A |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Vernal, Utah -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Laramie Regional Airport, WY (LAR/KLAR) |
Destination airport: | Provo Airport, UT (PVU/KPVU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot took off for his destination airport after waiting 2 hours at an intermediate stop due to weather. Approaching Vernal, Utah, the pilot said he encountered weather again. He deviated south and then back north trying to locate a path around the weather. He said he burned an hour's worth of fuel during the deviation. The pilot said he looked at his fuel and determined that he would need to land and get gas. The pilot said there was a layer of fog over the valley and over Vernal Airport. The pilot deviated first to Shane, Utah, then went to Roosevelt, Utah, and then back northeast toward Vernal. At that time he noted he had 7 gallons of fuel remaining. As the pilot was preparing to land at Vernal, the airplane ran out of gas on one tank. Approximately 4 miles southwest of the Vernal Airport, the pilot said he ran out of gas on the other tank. The pilot said he came out of the clouds 400 feet above a highway. He said there was mountainous terrain all around him. The pilot said he saw a plateau ahead. He said he pulled the airplane up and put it down on the plateau, breaking the landing gear aft and crushing the firewall and bottom fuselage upward and aft. An examination of the airplane revealed there was no fuel in either fuel tank. An examination of the engine and other airplane systems revealed no anomalies.
Probable Cause: the pilot's improper in-flight planning/decision. Factors contributing to the accident were fuel exhaustion and the fog.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN03LA021 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB DEN03LA021
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 05:56 |
ASN Update Bot |
Added |
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