ASN Wikibase Occurrence # 296405
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Date: | Saturday 23 November 2002 |
Time: | 16:30 LT |
Type: | Cessna 172K |
Owner/operator: | Stanley Haddix |
Registration: | N7192G |
MSN: | 17258892 |
Year of manufacture: | 1969 |
Total airframe hrs: | 3700 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Prestonsburg, Kentucky -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Paintsville, KY (3I6) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was in level flight at 3,000 feet, when the engine began to run rough. The pilot cycled the magneto switch and noted no changes in the engine performance. He then observed the oil pressure gauge in the "zero" position. The engine then lost total power, and a forced landing was performed to a field. When the engine was examined, a 2-inch hole in top of the engine crankcase was noted. The connecting rod and camshaft area of the number four cylinder has sustained extreme heating. The bottom half of the connecting rod was bent out of shape, with one of the rod end bolts remaining wedged in the rod end. The other rod end bolt was missing. No evidence of oil leakage was observed. The engine had accumulated about 2,400 hours of operation since it's last overhaul. An annual inspection of the engine was performed about 3 months prior to the accident. A 50-hour inspection, which included servicing the engine with 7 quarts of oil, was conducted 2 days prior to the accident.
Probable Cause: The loss of oil pressure for undetermined reasons, which resulted in a failure of connecting rod end bolts, due to an over temperature condition.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC03LA023 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB NYC03LA023
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 06:02 |
ASN Update Bot |
Added |
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