ASN Wikibase Occurrence # 296417
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Date: | Wednesday 20 November 2002 |
Time: | 16:00 LT |
Type: | Piper PA-28R-201 |
Owner/operator: | Salt Lake Community College |
Registration: | N850FS |
MSN: | 2844080 |
Year of manufacture: | 2002 |
Total airframe hrs: | 194 hours |
Engine model: | Lycoming IO-360-C1C6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tooele, Utah -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | Salt Lake City International Airport, UT (SLC/KSLC) |
Destination airport: | Salt Lake City International Airport, UT (SLC/KSLC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the instructor, the purpose of the flight was to prepare the student for dual cross-country flights and to familiarize him with the Piper PA-28R-201. Prior to this flight, the student pilot had been flying a Diamond Alarus, a training type airplane. They flew to a nearby airport, where they made three touch and go landings. On the fourth touch and go landing, the student pilot "assertively retracted the gear without warning" instead of the flaps. The right main and nose landing gear retracted and the airplane veered off the right side of the runway. The right wing struck a taxiway light, spinning the airplane around, and the left side of the fuselage struck a taxiway sign. The right wing was wrinkled and there was a gash from the leading edge back to the spar. The prop blade was bent. The left side of the fuselage was also wrinkled and buckled. According to FAA inspectors who examined the airplane, the squat switch on the landing gear had been rigged incorrectly. The squat switch actuated at .625 inches, exceeding the airplane's service manual requirement by .375 inches, or 150 percent. There were no entries in the maintenance records entries involving the squat switch. The torque seal on the squat switch mounting screws showed no signs of being disturbed.
Probable Cause: the inadvertent retraction of the landing gear during landing roll by the dual student. Contributing factors included the dual student's lack of familiarity with the aircraft, inadequate supervision by the flight instructor, and improper rigging of the landing gear squat switch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN03LA017 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB DEN03LA017
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 06:08 |
ASN Update Bot |
Added |
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