ASN Wikibase Occurrence # 296551
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Date: | Sunday 6 October 2002 |
Time: | 15:15 LT |
Type: | SIAI-Marchetti SM.1019 |
Owner/operator: | Private |
Registration: | N2069W |
MSN: | NC 057 |
Total airframe hrs: | 1680 hours |
Engine model: | Allison 250-B15G |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Midland, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Demo/Airshow/Display |
Departure airport: | Midland International Air and Space Port, TX (MAF/KMAF) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane struck power lines during a forced landing following a loss of engine power during the takeoff/initial climb. The pilot reported that the engine lost power to flight idle then regained power momentarily; however, the engine would not gain enough torque to sustain flight. Examination revealed that the "B" nut was "finger" loose on the line going from the bleed air filter to the fuel control unit. According to the manufacturer's representative, the recommended torque specification was 80 inch-pounds for the "B" nut, and the engine "condition described [by the pilot] could be caused by a leak in the bleed air system." During the last conditional inspection, the fuel control unit was removed for overhaul and reinstalled, and the fuel control unit and all filters were checked. The mechanic, who performed the conditional inspection, stated that during his removal and reinstallation of the fuel control unit, he removed the fuel and bleed air lines at the fuel control unit. The airplane had flown approximately 5 hours since the conditional inspection. Numerous attempts to obtain the completed Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) were unsuccessful.
Probable Cause: The loss of engine power resulting from a loose "B" nut on the line going from the bleed air filter to the fuel control unit. Also causal was the inadequate maintenence of the fuel control unit and filters during the last conditional inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW03LA006 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB FTW03LA006
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 07:53 |
ASN Update Bot |
Added |
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