Accident Boeing 757-251 N534US,
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Date:Monday 9 September 2002
Time:21:46 LT
Type:Silhouette image of generic B752 model; specific model in this crash may look slightly different    
Boeing 757-251
Owner/operator:Northwest Airlines
Registration: N534US
MSN: 24265/196
Year of manufacture:1988
Total airframe hrs:47466 hours
Engine model:Pratt & Whitney 2037
Fatalities:Fatalities: 0 / Occupants: 103
Aircraft damage: Substantial
Category:Accident
Location:Baltimore/Washington International Airport, MD (BWI/KBWI) -   United States of America
Phase: Unknown
Nature:Passenger - Scheduled
Departure airport:Minneapolis-St. Paul International Airport, MN (MSP/KMSP)
Destination airport:Baltimore/Washington International Thurgood Marshall Airport, MD (BWI/KBWI)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The Boeing 757 was on a right downwind for runway 33L, with the captain as the flying pilot. The airplane was aligned with runway 33R, and the flight crew was informed by the control tower. The first officer suggested a go-around. However, the captain had runway 33L in sight and initiated a side-step maneuver when the airplane was about 500 feet AGL. The airplane was aligned with runway 33L about 4 seconds prior to touchdown, as the airplane passed through 50 feet AGL. The first officer thought the airplane was low and again suggested a go-around. However, the captain continued with the landing. When the pilot closed the throttles, the airplane struck the runway in a nose high pitch attitude, and damaged the rear pressure bulkhead. Both pilots reported that they were unaware that the speed brakes, which had been extended when the airplane left 5,000 feet on approach, were still extended at touchdown. Company procedures required the pilot's hand to remain on the speed brake lever while they were extended, and stabilized approach criteria required the airplane to be aligned with the intended runway of landing by 500 feet above the touchdown zone elevation. The captain reported that he planned on a reserve fuel of 7,200 pounds, but it was reduced to 5,800 pounds by delays, and altitude and airspeed restrictions. He estimated a go-around would take 2,000 pound, but upon further questioning admitted that number was consistent with a go-around in a Boeing 747, his previous assignment, and the Boeing 757 would burn less fuel. The captain had accumulated 142 hours in the Boeing 757.

Probable Cause: The captain's failure to follow existing company procedures for stabilized approach, and use of speed brakes.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC02LA187
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB NYC02LA187

Revision history:

Date/timeContributorUpdates
14-Oct-2022 09:09 ASN Update Bot Added

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