ASN Wikibase Occurrence # 296669
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Date: | Friday 6 September 2002 |
Time: | 09:10 LT |
Type: | Monnett Sonerai II L |
Owner/operator: | |
Registration: | N356RB |
MSN: | 1493 |
Total airframe hrs: | 23 hours |
Engine model: | Volkswagen 1834 c.c. |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Canton, Illinois -
United States of America
|
Phase: | Unknown |
Nature: | Test |
Departure airport: | Canton-Ingersoll Airport, IL (KCTK) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a forced landing following a partial loss of engine power, the pilot inadvertantly stalled on short final and the airplane was substantially damaged. The pilot reported that immediately after takeoff, the engine began to "sputter and lose r.p.m.'s". The pilot attempted to return to the airport, but was unable to maintain altitude and elected to execute a forced landing into a bean field approximately 200 feet east of the runway. The pilot reported installing a new carburetor which required an adapter to properly mate to the existing intake manifold. This was the first flight following installation. He reported that a full static run-up had been completed prior to takeoff and that two static run-ups were conducted in the days prior to the accident. A post-accident examination revealed that the flanges on the aircraft engine intake manifold and the carburetor mounting flange did not seal completely, causing an induction air leak at the carburetor mounting flange. In addition, one coil on the electronic ignition was found to be cracked and failed to produce a spark at its associated spark plugs.
Probable Cause: The partial failure of the ignition system, the induction air leak at the carburetor mounting plate, and the pilot's inadvertant stall during the forced landing. Contributing factors were the crack in the electronic ignition coil, and the improper installation of the carbuetor resulting in an induction air leak.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02LA274 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB CHI02LA274
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 09:21 |
ASN Update Bot |
Added |
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