ASN Wikibase Occurrence # 296720
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Date: | Tuesday 27 August 2002 |
Time: | 08:40 LT |
Type: | Wittman W-8 Tailwind |
Owner/operator: | |
Registration: | N3992A |
MSN: | 37 |
Engine model: | Lycoming O-235-C1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Albuquerque, New Mexico -
United States of America
|
Phase: | Unknown |
Nature: | Test |
Departure airport: | Albuquerque-Double Eagle II Airport, NM (KAEG) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported to the FAA inspector that the flight was being conducted to evaluate a recently installed ground adjustable propeller. After maneuvering for a short time, the pilot and his passenger decided to return to the airport to readjust the propeller pitch in order to improve the climb capabilities of the aircraft. While returning to the airport, the engine developed "a sudden and violent vibration," and the pilot immediately decided to shut down the engine. After the propeller stopped rotating, the pilot observed that one of the three propeller blades had separated from the hub. A forced landing was initiated into an open field located about 5.5 nautical miles west of the airport of departure. The pilot added that during the landing on a rough and uneven terrain, the airplane touched down hard at about a 1,200 feet per minute rate of descent. The main landing gears sunk into the soft sandy soil, and the tailwheel-equipped airplane nosed over and came to rest in the inverted position. The airplane was reported to be powered by a 115 horsepower Lycoming O-235-C1A engine. The engine was driving a 3-bladed Precision propeller, which according to the pilot had accumulated less than 3 hours since installed new on the engine. The propeller model and serial number were not provided by the pilot. The mode of failure of the propeller blade could not be determined. The 331-hour instrument rated private pilot reported having accumulated a total of 38 hours in the accident make and model aircraft.
Probable Cause: The structural failure and separation of a propeller blade for undetermined reasons. A contributing factor was the lack of suitable terrain available to the pilot to execute a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW02LA242 |
Status: | Investigation completed |
Duration: | 1 year and 9 months |
Download report: | Final report |
|
Sources:
NTSB FTW02LA242
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 09:57 |
ASN Update Bot |
Added |
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