ASN Wikibase Occurrence # 297180
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Date: | Saturday 8 June 2002 |
Time: | 12:45 LT |
Type: | Maule M-7-260C |
Owner/operator: | 63kp LLC |
Registration: | N63KP |
MSN: | 30029C |
Total airframe hrs: | 92 hours |
Engine model: | Lycoming IO-470-V4A5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fishers, Indiana -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Lebanon, IN (6I4) |
Destination airport: | Fishers, IN |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an attempted aborted landing the airplane impacted trees and terrain. The pilot reported, "Touchdown took place at about 1/2 of the way down the 1000' long field with a short bounce that put me uncomfortably long. I executed a go around and was surprised by the very sluggish climb performance and the height of the trees at the end of the field. I felt like the full flaps were creating too much drag at the same time I realized that I was perilously close to the pine trees at about 50 feet high. I retracted the flaps to reduce drag at about the same time that the right wing tip caught the pine. The impact slowed the right wing and the aircraft spun to the right coming down in the field north of the trees." The pilot stated, "In retrospect I realize that I had too much fuel 50 [gallons] versus my usual 25 [gallons] for this field and that the temperature and high humidity increased my ground speed due to the higher density altitude and drastically reduced my climb performance where my previous landings here [were] in the winter at much cooler temperatures. The turbulence and gusts caused me to add too much airspeed for a successful short field landing taking into account the power line." A weather reporting station recorded the wind speed around the accident time as 6 knots with no gusts.
Probable Cause: The pilot not performing a go-around prior to exceeding the proper touchdown point and the pilot not maintaining altitude/clearance from the trees. Factors to the accident were the pilot's inadequate preflight planning and the trees.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02LA157 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB CHI02LA157
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 15:26 |
ASN Update Bot |
Added |
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