ASN Wikibase Occurrence # 297200
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Date: | Tuesday 4 June 2002 |
Time: | 21:00 LT |
Type: | Beechcraft BE-100-A100 |
Owner/operator: | Chris Finkbeiner |
Registration: | N799DD |
MSN: | B-102 |
Year of manufacture: | 1972 |
Total airframe hrs: | 8400 hours |
Engine model: | Pratt & Whitney PT6-28 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Little Rock, Arkansas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Little Rock-Bill and Hillary Clinton National Airport, AR (LIT/KLIT) |
Destination airport: | Little Rock-Bill and Hillary Clinton National Airport, AR (LIT/KLIT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was on a practice approach when he extended the landing gear. The cockpit gear indicators yielded "two" green indications. A go-around was performed and the gear cycled several times with no results, including an attempt to use the emergency extension system. Two confirmation passes were performed, and it was confirmed that the left main landing gear was retracted with the nose and right main landing gear extended. After touch down on the right side of the runway, the aircraft exited the left side of the runway. Examination of the aircraft revealed that left gear extension push/pull tube was found without the lock pin in its clevis. The pin was found in the belly of the aircraft but no nut and washer was found. The aircraft had recently come out of a maintenance facility where the landing gear was worked on.
Probable Cause: The malfunction of the left main landing gear retraction/extension assembly due to a missing lock pin/washer/nut on the clevis of the push/pull gear extension tube that resulted from improper maintenance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW02LA172 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB FTW02LA172
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 15:39 |
ASN Update Bot |
Added |
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