Accident Bell 206B-III N191RH,
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ASN Wikibase Occurrence # 297265
 
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Date:Thursday 23 May 2002
Time:18:25 LT
Type:Silhouette image of generic B06 model; specific model in this crash may look slightly different    
Bell 206B-III
Owner/operator:Shier Aviation Corp
Registration: N191RH
MSN: 3177
Year of manufacture:1980
Total airframe hrs:4798 hours
Engine model:Allison 250 C-20 B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Moab, Utah -   United States of America
Phase: Unknown
Nature:Ferry/positioning
Departure airport:Harely B Ranch, UT
Destination airport:Moab, UT
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
According to the pilot, he started the day with approximately 50 gallons of fuel on board. He departed from his home base, for a 10 minute flight to pick up several passengers, taking groups of them on 5 to 10 minute photo flights, for a total mission duration of approximately 80 to 90 minutes. After dropping off the last group, he returned to his home base. According to the fuel gauge, there was approximately 12 to 13 gallons of fuel remaining when he departed for the 10 minute repositioning flight back to his home base. Based on a fuel burn rate of approximately 25 gallons per hour, he calculated that he had 30 minutes of fuel remaining. He also stated that, due to noise abatement, he always approached his helipad at a "high airspeed and with a fast rate of descent and then about 100 feet, power up to make a high power, steep landing." Being "low on fuel," he did the same thing on this approach, starting his descent at approximately 80 to 100 knots. At 50 to 75 feet above ground level (agl), he initiated a 10 to 20 degree flare and began the descent to land. The fuel boost pump light illuminated, the "auto-relight" light came on, and the "engine out" light illuminated. His first thought was that he "ran the aircraft out of fuel." He realized that he was going too fast to land at his helipad. He adjusted his approach, and attempted to land in a parking lot just beyond his pad. He applied forward cyclic control, to level out the helicopter, hoping the boost pump light would go out and that the "auto relight" would reignite the fuel if it started pumping. The helicopter struck the ground hard with its right landing gear skid, bounced, slid forward approximately 15 feet, turned to its left approximately 90 degrees and slowly rolled over on its right side. The aircraft continued to turn to the left another 90 degrees and came to rest on its right side, facing 180 degrees from the direction of the approach. During the hard landing, the main rotor blades struck the tail boom, separating the vertical stabilizer, tail rotor and tail rotor gearbox. The main rotor hub and blade assembly was intact and remained attached to the main rotor mast.

Probable Cause: The pilot's failure to maintain rotor rpm during a forced landing. A contributing factor was fuel starvation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN02LA046
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB DEN02LA046

Revision history:

Date/timeContributorUpdates
14-Oct-2022 16:27 ASN Update Bot Added

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