ASN Wikibase Occurrence # 297273
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Date: | Tuesday 21 May 2002 |
Time: | 23:05 LT |
Type: | Cessna 172N |
Owner/operator: | Split S Aviation |
Registration: | N734KG |
MSN: | 17268909 |
Year of manufacture: | 1977 |
Total airframe hrs: | 14278 hours |
Engine model: | Lycoming O-320-H2AD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Glen Rose, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Fort Worth, TX (T67) |
Destination airport: | San Antonio International Airport, TX (SAT/KSAT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the dark night cross-country flight, while at a cruise altitude of 2.000 feet msl, the pilot initiated a climb to 3,000 feet. A few minutes later, the engine's rpm dropped 200-300 rpm. The 67-hour pilot increased throttle to check for an rpm response. Subsequently, the engine lost power, and a forced landing was initiated. While approaching to land, the pilot noticed trees in front of the airplanes flight path and started looking for another place to land, but couldn't see anything because it was too dark. Subsequently, the aircraft impacted tress coming to rest upright. An examination of the engine under the supervision of an FAA inspector, revealed the left magneto's internal gears did not rotate with the engine. Removal of the left magneto revealed only one of two rubber drive isolators inside the ignition harness cap. Internal inspection revealed the contact points on the left hand side of the magneto did not open on rotation. Further examination of the airplane, displayed the ignition key turned to the left magneto only. The pilot reported to the NTSB investigator-in-charge, that he did not touch any switch while exiting the aircraft.
Probable Cause: The pilot's failure to set the ignition key to the both magnetos position, which resulted in a loss of engine power. Contributing factors were the failure of the left magneto, the lack of suitable terrain for the forced landing, and the dark night.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW02LA159 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB FTW02LA159
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 16:33 |
ASN Update Bot |
Added |
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