ASN Wikibase Occurrence # 297283
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Date: | Sunday 19 May 2002 |
Time: | 10:54 LT |
Type: | Cessna 150G |
Owner/operator: | Robert Frank |
Registration: | N8657J |
MSN: | 15066557 |
Year of manufacture: | 1967 |
Total airframe hrs: | 2083 hours |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kenosha, Wisconsin -
United States of America
|
Phase: | Unknown |
Nature: | Training |
Departure airport: | CHICAGO/PROSPEC, IL |
Destination airport: | Kenosha-Kenosha Municipal Airport, WI (ENW/KENW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was damaged during a forced landing to a plowed field following a loss of engine power while approaching to land. The airplane was being flown by a certified flight instructor (CFI) and a student pilot. The CFI stated that prior to the flight the student pilot performed a sump check of the fuel tanks and found water in the fuel samples. She said that she instructed the student to sump the fuel tanks three to five times, after which they were able to get clear fuel samples. The CFI stated that she and her student checked the weather and decided to practice landings at ENW. The CFI said that they were set up for a straight-in approach to runway 6R at ENW when the engine lost power. She said that she assumed control of the airplane and performed a, "...flow check: (Fuel selector - Both, Mixture - Rich, Carb heat - ON, Throttle - Set, [Magnetos] - Both, Engine gauges - Green.)" The CFI reported that she determined that she would not be able to make the runway and she elected to land in a field. During the forced landing, the nose landing gear of the airplane collapsed. A postaccident examination of the airplane revealed traces of water in the fuel tanks, fuel hoses, and the carburetor. No other anomalies were found that could be determined to have existed prior to the accident. The temperature and dewpoint at the time of the accident were reported as 8 degrees Celsius and 3 degrees Celsius respectively. According to a carburetor icing chart, the temperature and dewpoint are within the range of serious icing potential for any power setting. Federal Aviation Administration Advisory Circular 20-113 states the following regarding the use of carburetor heat: "[Carburetor] Heat should be applied for a short time to warm the induction system before beginning a prolonged descent with the engine throttled and left on during the descent. Power lever advancement should be performed periodically during descent to assure that power recovery can be achieved. The pilot should be prepared to turn heat off after power is regained to resume level flight or initiate a go-around from an abandoned approach."
Probable Cause: The student pilot's failure to use carburetor heat, and the flight instructor's inadequate supervision of the flight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02LA138 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB CHI02LA138
Revision history:
Date/time | Contributor | Updates |
14-Oct-2022 16:44 |
ASN Update Bot |
Added |
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